TL* THE CONTACT OWNS A 2008 MAZDA CX9. THE CONTACT WAS DRIVING APPROXIMATELY 15 MPH WHEN THE STEERING WHEEL BECAME EXTREMELY STIFF. THE CONTACT WAS UNABLE TO MAINTAIN CONTROL OF THE VEHICLE AND WAS INVOLVED IN A CRASH WITH ANOTHER VEHICLE. THE DRIVER WAS INJURED. A POLICE REPORT WAS AVAILABLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT REPAIR FACILITY WHERE REPAIRS WERE MADE TO THE BODY DAMAGE. PRIOR TO THE CRASH, THE CONTACT WAS ADVISED BY AN AUTHORIZED DEALER THAT THE VEHICLE EXHIBITED A POWER STEERING FLUID LEAK. THE DEALER WAS UNABLE TO MAKE REPAIRS BECAUSE THE PARTS NEEDED WERE NOT READILY AVAILABLE AND ON BACK ORDER. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 33,000 AND THE CURRENT MILEAGE WAS UNKNOWN.
2009
EXTERIOR LIGHTING
THE LOW BEAM HEADLAMP CONNECTOR ON THE PASSENGER SIDE MELTED INSIDE THE HEADLIGHT CAUSING THE LIGHT TO FAIL. NOW THE DRIVER SIDE HAS DONE THE EXACT SAME THING CAUSING THE LIGHT TO FAIL. THIS COULD CREATE A SERIOUS INJURY AND REQUIRES THE REPLACEMENT OF A DEFECTIVE LIGHT CONNECTOR. *TR