Other Engine Info: Engine Type: 24V, Sales Code: EER
Other Restraint System Info: Restraint System Active Driver and Passenger Air Bags (CGW) ( LH Family Only)
Plant City: Brampton
Plant Company Name: Brampton Assembly
Plant Country: Canada
Plant State: Ontario
Seat Belts All: Manual
Series: LH
Series2: H (High Line)
Trim: LX
Valve Train Design: Dual Overhead Cam (DOHC)
Vehicle Type: PASSENGER CAR
Model year
COMPONENT
Complaint
2000
ENGINE AND ENGINE COOLING:ENGINE
INTERMITTENTLY WHILE STARTING THE VEHICLE CONSUMER HEARD A SCREECHING NOISE COMING FROM THE ENGINE. WHILE THE NOISE WAS PRESENT VEHICLE REVVED SEVERELY. AFTER AWHILE THE NOISE SUBSIDED, AND THE RPMS WOULD LOWER SIGNIFICANTLY. SEVERAL MONTHS LATER CONSUMER STARTED THE VEHICLE AND HEARD A DISCOURAGING SOUND. ENGINE SOUNDED AS IF THERE WAS A HAND FULL OF TACKS BEING GROUNDED UP. DEALER EXAMINED THE VEHICLE, AND INFORMED THE CONSUMER THAT THE TIMING CHAIN SNAPPED, AND THE ENGINE NEEDED TO BE REPLACED. *AK THE MANUFACTURER REFUSED TO PAY FOR THE REPAIRS ALTHOUGH THE VEHICLE HAS AN EXTENDED WARRANTY. THE CONSUMER DIDN'T HAVE THE $5900. TO REPAIR THE VEHICLE SO THEY TRADED IT IN. *NM
2003
EXTERIOR LIGHTING
MY 2003 CONCORDE SHUT OFF ON ME WHILE DRIVING TO WORK ON 695 EXPRESSWAY. THE ENGINE LIGHT CAME ON AND I STARED TO LOSE POWER. ON 06/30/08 QUICKLY I PUT MY CAR INTO NEUTRAL AND IT STARTED BACK UP AND CONTINUE TO WORK BUT WOULD NOT GO PASS 60 MPH. LUCKY FOR ME THERE WAS NO HEAVY TRAFFIC OR I COULD HAVE BEEN SERIOUSLY HURT. THERE WAS NO SIGN THAT THE CAR WAS GOING TO LOSE POWER AS SOON AS THE LIGHT POP ON THE CAR STARTED TO LOSE POWER. I TOOK THE CAR TO A DEALERSHIP FOR SERVICE AND AT THAT TIME THEY TOLD ME THAT IT WAS A SHORTED UPSTREAM 02 SENSOR . I PARKED THE CAR AND DID NOT DRIVE THE CAR UNTIL 09/27/08 TO THE DEALERSHIP THE CAR WAS REPAIRED. ON 09/29/08 AFTER DRIVING THE CAR FOR 12 MILES THE LIGHT THEN POP BACK ON AGAIN AND THE SAME THING HAPPEN IT SHUT OFF WHILE I WAS DRIVING. I TOOK THE CAR BACK TO THE DEALERSHIP AT THIS TIME THEY TOLD ME THERE WAS A CODE THAT CAME DURING THE TEST STATED THAT THE CAT CONVERTER INTERNAL WAS DEFECTIVE AND THE DOWN STREAM 02 SENSOR. I HAD THAT REPLACED. ON 10/02/08 AFTER THAT REPAIR I DROVE ANOTHER 24 MILES THIS TIME AND AS USUAL THE LIGHT POP BACK ON AGAIN BUT THIS TIME THE CAR SOUND AS IF IT WAS IN NEUTRAL OR DIFFERENT SHIFT AND WOULD NOT PICK UP SPEED WITH A ROARING LOUD NOISE. I THEN PULL OVER TO THE SHOULDER AND TURN THE CAR OFF AND THEN BACK ON AGAIN AND IT CONTINUE TO DRIVE NORMAL. ENGINE LIGHT CONSTANTLY STAYED ON. I RETURNED THE CAR BACK TO THE DEALERSHIP FOR REPAIR AT THIS TIME THEY SAID A DIFFERENT CODE APPEAR AND SAID THE P0420,PO430 AND THEY ORDER A ED CAT CONVERTER AND NOW THE LEFT UPSTREAM 02 SENSOR. WHICH THEY HAD ALREADY REPLACED THE RIGHT CONVERTER AND BOTH SENSORS NOW THEY ARE WORKING ON THE LEFT. CAR WAS REPAIRED ON 10/06/08 AFTER THAT REPAIR I DROVE THE CAR TO WORK AND ON THE WAY HOME THE ENGINE LIGHT POP BACK ON FOR THE THIRD TIME, TOOK THE CAR BACK TO THE DEALERSHIP AND NOW THE CODE SAY PO600 AND THE PCM AND SOLENOID WAS PROGRAMMED AND REPLACED. NOW I HAVE TO GET UP AT 6AM TO TAKE THE CAR BACK. *TR