CONSUMER WAS TOLD THAT WRONG SIZE GAS TANK IS EQUIPPED ON VEHICLE. *AK PREMATURE CLUTCH FAILURE, DRIVESHAFT FAILURE. BOLTS VIBRATED OUT OF EXHAUST NAMIFOLD. RECURRING NOISE FROM ENGINE PULLEY AREA. *SLC
1998
ENGINE AND ENGINE COOLING:ENGINE
EXHAUST BOLTS VIBRATED LOOSE/BROKE OFF (7/15/98;1/4/99;11/19/99) IDLER PULLEY HAS BEEN CHANGED 3 TIMES(1/4/99;11/17/99;11/19/99); DRIVE BELT HAS BEEN REPLACED 2 TIMES(1/15/99;11/19/99); MOTOR MOUNTS NEEDED TO BE SECURED (2/26/99); CLUTCH SLAVE CYLINDER NEEDS TO BE REPLACED (COMPLAINED 7/15/98;1/25/00. DIAGNOSED 6/12/00); NOISE COMING FROM TRANSMISSION(6/12/00 TOLD NOISE NORMAL); DRIVESHAFT CV JOINT BAD (6/12/00 TOLD BY DEALER NOISE NORMAL. 6/14/00 TOLD DRIVESHAFT CV JOINT BAD DUE TO POOR DESIGN. 6/16/00 2ND ESTIMATE DRIVESHAFT CV JOINT BAD). THE MANUFACTURER HAS BEEN NOTIFIED NUMEROUS TIMES BUT CONTINUES TO STONEWALL REGARDING ISSUES WITH MY CAR. *AK ALSO WRONG , SMALLER SIZE GAS TANK WAS INSTALLED VEHICLE. MANFACTURER IS NOT SENDING NHTSA INFORMATION REGARDING TSB OR RECALLS.