I OWN AN '02 CHEVY MALIBU (SINCE 2/28/02). I HAD THE SAME HAZARD SWITCH PROBLEM W/MY '02 MALIBU THAT THE '00 & '01 MODEL YEARS HAD, AND I HAD TO PAY FOR ITS REPLACEMENT (ROUGHLY $130). I HAD NO TURN SIGNALS OR HAZARD BLINKERS UNTIL IT WAS REPLACED. GIBSON CHEVY OF SOUTH HOLLAND, IL DID THE REPLACEMENT (IT'S IN THEIR REPAIR SYSTEM). MY CAR PRESENTLY HAS A LITTLE OVER 45K MILES. GM SHOULD REIMBURSE ME FOR THE MONEY I WAS FORCED TO PAY, GIVEN THE HISTORY OF THIS DEFECT WITH PRIOR MODEL YEARS AND THE FACT THIS SITUATION HAS NOT SEEMINGLY BEEN REPLACED WITH THE '02 MODEL YEAR, EITHER. I GOT NO NOTIFICATION OF A PROBLEM WITH THIS SWITCH OR A RECALL ON IT, EITHER. I HAVE HAD TO HAVE A MODULATOR REPLACED LAST WEEK (10/5/05) WHICH AFFECTS THE BLOWER MOTOR SPEEDS IN MY VEHICLE'S VENTILATION SYSTEM ($152.00). AT SPEEDS 1, 2 AND 3, THE BLOWER MOTOR WOULDN'T WORK AT ALL. EACH SPEED STARTING WITH THE LOWEST TO THE HIGHER SPEEDS WAS GOING OUT-THE ONLY SPEEDS WORKING WERE #4, #5 & DEFROST. I WAS FORCED TO HAVE THIS REPLACED OR I WOULDN'T BE ABLE TO USE THE VENTS OR DEFROSTER OR THE BLOWER ITSELF (& THE DEFROSTER), WOULD NOT WORK AT ALL. THIS REPAIR WAS DONE AT BRACH AUTO REPAIR (103RD & WESTERN AVE., CHICAGO IL -- THIS REPAIR DETAIL IS IN THEIR SYSTEM). BRACH AUTO ALSO REPLACED SOME PARTS IN MY FUEL INJECTION SYSTEM (IT WAS MALFUNCTIONING/ABOUT TO GO OUT). THE AMT I PAID FOR THIS IS ALSO IN THEIR SYSTEM. AT THAT TIME, TOM BEAULIEU INFORMED ME THAT GM HAS DISTRIBUTED A TSB RE: THIS SITUATION (WHICH I WAS NOT INFORMED OF UNTIL I TOOK MY CAR IN FOR THE MODULATOR REPAIR), & HOW I MUST RUN MY CAR W/ ONLY SHELL OR BP'S 93 OCTANE GASOLINE (EVEN THOUGH THE OWNER'S MANUAL STATES IT SHOULD/CAN RUN ON 87 OCTANE). NOW, DUE TO A POOR FUEL INJECTOR DESIGN, RUNNING ANYTHING LESS THAN 93 OCTANE IN MY '02 MALIBU WILL RESULT IN MORE COSTLY REPAIRS. (3 SEPARATE FAILURES / 3 SEPARATE PARTS ON THE SAME CAR). I WANT GM TO REIMBURSE ME FOR THE MONEY I'VE SPENT FOR THESE REPAIRS.*JB
2007
ELECTRICAL SYSTEM
2007 CHEVROLET MALIBU. CONSUMER WRITES IN REGARDS TO DRIVER DOOR LOCK MALFUNCTION CAUSED BY POOR WIRE CONNECTION AND CONSUMER SEEKS REIMBURSEMENT FOR REPAIRS. *SMD THE CONSUMER STATED WHILE DRIVING, THE TIRE TRACTION LIGHT ILLUMINATED AND HE WAS UNABLE TO TURN IT OFF, AND THEN THE CHECK ENGINE LIGHT ILLUMINATED. HE WAS ALSO UNABLE TO USE THE SPEED CONTROL SETTING, DURING THAT TIME. WHEN HE ARRIVED HOME, HE WAS UNABLE TO GET OUT OF THE VEHICLE, BECAUSE THE DRIVER DOOR AUTO LOCK WOULDN'T OPERATE PROPERLY. TWO DAYS LATER, WHEN HE PUT THE VEHICLE INTO DRIVE, THE DRIVER SIDE DOOR DIDN'T LOCK AUTOMATICALLY, BUT ALL THE OTHER LOCKS WORKED PROPERLY. THE DEALER INFORMED THE CONSUMER THE HARNESS CAME LOOSE AND IT CAUSED THE WIRING UNDER THE DRIVER'S SEAT TO CHAFF AND EXPOSE THE WIRING WHICH THEN TOUCHED EACH OTHER AND CAUSED THE MALFUNCTION. HE FURTHER ADVISED THAT, AS PART OF THE REPAIR, THE HARNESS AND WIRING WERE MOVED OVER FROM ITS ORIGINAL LOCATION SO THAT THE PROBLEM WOULD NEVER OCCUR AGAIN.