GVWR: Class 1B: 3,001 - 4,000 lb (1,360 - 1,814 kg)
Make: ACURA
Manufacturer: HONDA MOTOR CO., LTD
Manufacturer Id: 987
Model: RSX
Model Year: 2004
Plant City: Suzuka
Plant Country: Japan
Plant State: Mie
Seat Belts All: Manual
Transmission Speeds: 6
Transmission Style: Manual/Standard
Trim: Type-S
Valve Train Design: Dual Overhead Cam (DOHC)
Vehicle Type: PASSENGER CAR
Model year
COMPONENT
Complaint
2003
VEHICLE SPEED CONTROL
TL*THE CONTACT OWNS A 2003 ACURA RSX WITH A 4-CYLINDER, 2.0 LITER ENGINE. WHILE DRIVING AT SPEEDS OF 65 MPH, THERE WAS A TAPPING NOISE COMING FROM UNDER THE HOOD. THE VEHICLE THEN STALLED WITHOUT WARNING AND SHORTLY AFTER, HE WAS ABLE TO RESTART THE VEHICLE. ONCE THE VEHICLE WAS RESTARTED, THE VEHICLE ABNORMALLY ACCELERATED AND INCREASED IN ENGINE RPMS OF 9,000. HE WAS ABLE TO PUT THE VEHICLE INTO NEUTRAL AND MANEUVER OFF THE HIGHWAY. THE ENGINE THEN BLEW ITSELF AND MADE A LOUD POPPING NOISE. HE WAS UNABLE TO RESTART THE VEHICLE AT THAT POINT. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THEY PERFORMED A DIAGNOSTIC AND DETERMINED THE FAILURE TO BE DRIVER ERROR. THE ENGINE WAS REPLACED AT THE OWNER'S EXPENSE. THE FAILURE AND CURRENT MILEAGES WERE APPROXIMATELY 86,000.
2004
POWER TRAIN:MANUAL TRANSMISSION
TL*THE CONTACT OWNS A 2004 ACURA RSX. WHILE DRIVING BETWEEN 65-70 MPH, THE TRANSMISSION BEGAN TO SLIP OUT OF GEAR FOLLOWED BY A LOUD GRINDING NOISE WHEN THE ACCELERATOR PEDAL WAS DEPRESSED. WHEN THE CONTACT WOULD DOWNSHIFT TO A LOWER GEAR, THERE WAS A LOW POWER RESPONSE AND A GRINDING NOISE WAS HEARD. THE FAILURES OCCURRED INTERMITTENTLY. OVER AN EXTENDED PERIOD OF TIME, THE FAILURES INCREASED WHILE THE VEHICLE WAS IN OPERATION. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER FOR INSPECTION, BUT THEY COULD NOT DUPLICATE THE FAILURES. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER ON TWO SEPARATE OCCASIONS, BUT THERE WERE NO RESOLUTIONS. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC AND THE TRANSMISSION WAS REPLACED. APPROXIMATELY FOUR MONTHS LATER, THE TRANSMISSION FAILED WITHOUT WARNING. THE VIN WAS UNKNOWN. THE FAILURE MILEAGE WAS 30,000 AND CURRENT MILEAGE WAS 60,000.